The incident occurred on Draugen in connection with a wireline operation in a well. The well was completed and started producing in 1994. Since January 2010, the well has been shut-in. Planning for the wireline operation started in the 4th quarter of 2009. During a planned test, it was discovered that the hydraulically operated main valve in the Xmas tree was not tight, which would entail repair or replacement. The wireline operation was therefore postponed until the main valve had been fixed. At the end of November 2010, the main valve had been repaired, and the implementation of the planned wireline operation could start again.
Stevedore Injury During Cargo Operations – Investigation Report
On 20 February 2006, a team of Stevedores was engaged in the discharge of steel products from the starboard side of No. 2 hatch of a Cargo Ship which was starboard side to at Jellicoe wharf in Auckland. The team consisted of a Foreman Supervisor and three Stevedores within the ships hold, a Hatchman on deck and a driver operating the ship’s crane.
Alexander L. Kielland Platform Capsize Accident – Investigation Report
The semi-submersible “flotel” (floating hotel) Alexander L. Kielland capsized on 27 March 1980 while bridge connected to the steel jacket Ekofisk Edda platform. The flotel lost one of its five legs in severe gale force winds, but not an extreme storm. The accident started with one of the bracings failing due to fatigue, thereby causing a succession of failures of all bracings attached to this leg. It was discovered during the investigation that the weld of an instrument connection on the bracing had contained cracks, which had probably been in existence since the rig was built. The cracks had developed over time, and the remaining steel was less than 50%.
Palletised Reefer Cargo Gear Failure – Investigation Report
At approximately 1140 hours New Zealand Daylight Time (NZDT) on 15 October 2004, vehicles were being discharged from a reefer vessel. Two gangs from the stevedoring company were operating on board at the time. At about 1140 hours, a 0.5 tonne lifting frame was lifting an approximate 1.0 vehicle from No. 3 hold. The stevedore operating the winch observed the starboard runner wire was starting to unravel. The winch driver immediately lowered the port runner allowing the vehicle to drop onto the starboard deck, as the wire on the yardarm of the union purchase parted.
Offshore Well Blowout – Investigation Report
A blowout occurred on a Well during the period from May 9 to May 18, 2001, after the 13⅜–inch surface casing was cemented. The mobile offshore drilling unit (MODU) was cantilevered over “Platform A.” The plan called for the well to be directionally drilled with a drift angle of approximately 55 degrees. On May 8, 2001, after the 13⅜-inch surface casing was cemented, a slight flow was noted coming from the annulus between the surface casing and the 18⅝-inch conductor casing. The diverter was closed and pressure started increasing on the annulus. Valves and piping were rigged up to the 18⅝-inch A section to permit monitoring of pressure and transport of fluids to and from the annulus. Throughout the night of May 8 and through 0730 hrs on May 10, unsuccessful attempts were made to bleed off the annular pressure.
Fatal Bulk Carrier and Cargo Ship Collision – Investigation Report
At about 2251 local time on 17 March 2007, a Hong Kong general cargo ship collided with a Chinese registered bulk carrier. At the time of the accident, the weather conditions were fine with northerly wind at force 4. The sea was moderate and the visibility was about 7 nautical miles (n.m.). The Bulk Carrier sustained damages to the bow and the Cargo Ship sank shortly after the collision. Twelve crew members of the Cargo Ship were rescued. Eight crew members were found missing and nine crew members were drowned.
Fatal Fall from Offshore Platform – Investigation Report
On the morning of May 19, 2000, a contract employee was using a portable of Accident winch (come-along) to remove a section of removable guardrail for the purpose of accommodating the installation of the mounting beams of a temporary crane. One end of the come-along was attached to the section of guardrail to be removed, while the other end was attached to a section of fixed guardrail located approximately 5 feet above the guardrail to be removed. As tension was applied to the come-along, the upper guardrail failed at its base welds and detached from the deck. As a result of the detachment, the employee fell approximately 60 feet to the Plus 10 deck and sustained fatal injuries.
Loss of Well Control Due to Leak from Seal Ring – Investigation Report
At approximately 1740 hours on February 14, 2008, a seal ring on the bottom flange below the master valve began to leak and dry gas was released into the atmosphere. Since the SCSSV was not operable and the leak was below the master valve, it was not possible to prevent the escape of natural gas. The South Pelto No. 10 platform was evacuated shortly after the loss of well control without injury. The Well was secured on February 17, 2008.